Example 
    High Gas Flow With MIG Welding Causing Erratic Arc, Some Might Call Arc Blow
    
    
    An interesting situation shows what can happen if excess shielding gas flow is 
    used.  An experienced field 
    Welding Engineer was testing a new model multiprocess power source in a fabricators 
    shop.  It worked fine in the Stick and TIG mode.  However when he switched 
    to MIG welding with a cylinder of 75% Argon 25% CO2 gas the arc was 
    harsh, erratic and  the spatter was very high with poor weld surface 
    appearance.  After checking grounding, polarity and 
    making settings changes with no improvement he called the power supply manufactures Product Manager.  After 
    discussing the problem, the Product Manager wondered about the gas flow rate 
    and asked to have it checked.  The field Welding Engineer said it was set for 
    30 (he assumed CFH.)  The Product 
    Manager had experience with poor performance when flow rates were set 
    excessively high.  He asked the field Welding Engineer to put the MIG 
    gun 
    nozzle up to his cell phone and pull the trigger with the wire disconnected!  The solution was 
    evident from the sound this very experienced Product Manager heard - the 
    flow was excessive!  Sure enough, the distributor salesman who set-up 
    the installation had used a standard inert gas regulator.  It was not a 
    Regulator/Flowgauge with an outlet orifice and flow calibrated pressure 
    gauge.  It was reading 30 psi not 30 CFH!  What flow were they 
    getting?  No doubt over 150 CFH.
 interesting situation shows what can happen if excess shielding gas flow is 
    used.  An experienced field 
    Welding Engineer was testing a new model multiprocess power source in a fabricators 
    shop.  It worked fine in the Stick and TIG mode.  However when he switched 
    to MIG welding with a cylinder of 75% Argon 25% CO2 gas the arc was 
    harsh, erratic and  the spatter was very high with poor weld surface 
    appearance.  After checking grounding, polarity and 
    making settings changes with no improvement he called the power supply manufactures Product Manager.  After 
    discussing the problem, the Product Manager wondered about the gas flow rate 
    and asked to have it checked.  The field Welding Engineer said it was set for 
    30 (he assumed CFH.)  The Product 
    Manager had experience with poor performance when flow rates were set 
    excessively high.  He asked the field Welding Engineer to put the MIG 
    gun 
    nozzle up to his cell phone and pull the trigger with the wire disconnected!  The solution was 
    evident from the sound this very experienced Product Manager heard - the 
    flow was excessive!  Sure enough, the distributor salesman who set-up 
    the installation had used a standard inert gas regulator.  It was not a 
    Regulator/Flowgauge with an outlet orifice and flow calibrated pressure 
    gauge.  It was reading 30 psi not 30 CFH!  What flow were they 
    getting?  No doubt over 150 CFH.  
     Even 
    with a 5/8 inch MIG gun nozzle, much more than about 50 to 60 CFH will cause 
    turbulent flow and mix air into the shielding gas stream!  It takes 
    only a small amount of  air to produce a less stable arc with excess 
    spatter and internal weld porosity-if it is not visible! Very high flows, as 
    in this situation, can cause to arc to "Blow" sideways or erratically. 
    Perhaps more harmful than the visible defects is the effect of Nitrogen on 
    the weld deposit.
Even 
    with a 5/8 inch MIG gun nozzle, much more than about 50 to 60 CFH will cause 
    turbulent flow and mix air into the shielding gas stream!  It takes 
    only a small amount of  air to produce a less stable arc with excess 
    spatter and internal weld porosity-if it is not visible! Very high flows, as 
    in this situation, can cause to arc to "Blow" sideways or erratically. 
    Perhaps more harmful than the visible defects is the effect of Nitrogen on 
    the weld deposit. 
    Note: In the above example, when the proper 
    regulator/flowgauge was installed, MIG weld performance was fine!
     See What That 
    Can Cause.